1. Airforce Aviation Repair Institute of Technology, Changsha 410242, China;
2. Aeronautical Service Sergeant School, Air Force Engineering University, Xinyang 464000, China;
3. Naval Aviation University, Yantai 264001, China
In order to reduce the axial force of the pneumatic drilling on the aircraft titanium alloy skin crack hole, the pneumatic drilling force test system was constructed, and the orthogonal test and the parameter optimization test of drilling force were carried out. Experimental results show that the effect of the axial force on the pneumatic drilling is in the order of velocity feed ratio(v/f),drill bit shape and lubrication conditions. When the S-type drill of W6Mo5Cr4V2Al is used to drill the 2mm thickness titanium alloy TC4 sheet, the motor cutting speed can be adjusted to 445-865 r/min, and the composite droplet jet lubrication (CMJ) is used. The lubrication parameter is set to atomization gas pressure of 0.4MPa, oil consumption of 80-100mL/h, water consumption of 200-400mL/h better.
黄登红,高昆,黄浩然,吕勤云,郁大照. 飞机钛合金蒙皮复合喷射润滑的气动钻削力试验研究[J]. 航空制造技术, 2018, 61(7): 97-101.
HUANG Denghong, GAO Kun, HUANG Haoran, Lü Qinyun, YU Dazhao. Study on Pneumatic Drilling Force Test of Compound Jet Lubrication Used in Titanium Alloy Thin-Walled Structure of Plane[J]. Aeronautical Manufacturing Technology, 2018, 61(7): 97-101.